Hi Brother,
I have a problem. Here i give the step by step what i do.
1. I connect receiver wiring.
2. I connect all 4 motors wiring correct as per diagram M1 to M4
3. Trim the YAW in 0
4. Transmitter ( HK T6A V2 - 6 ch Mode 2 ) switch ON
5. Throttle stick UP position
6. Connect the Battery, & Blink the blue LED 3 time & all calibration process ok ( Tx switch on position )
7.Then Down the Throttle.,
8. While UP the Throttle ., all the motors runs as per diagram.( clock ,Anti,clock,Anti)
9. Disconnect the battery., ( Tx switch on position )
10. YAW in Maximum position ( Tx switch on position )
11. connect the battery - ( Then all motors vibrate with beep sound ) ( Here is my big problem )
12. Increase the throttle ., Nothing Happen of M1 to M4
13.The Kk5.5 board goes on calibration mode( Here is my big problem ) so pl solve the problem & pm me.
I make this calibration step in 8 times., But nothing happen
smithraj