I have assembled at quad 450 size frame with naze32 full. the transmitter Im using is Turnigy 9x with stock firmware,
problem is when I connect the controller to the Receiver. and checked when I moved the throttle, pitch is moved on cleanflight. and when I move the pitch on transmitter, throttle is moved in cleanflight.
then I interchanged the wires on receiver. then everything was showing fine. but when I try to fly the quad, it flips before takeoff. I checked everything, motors are turning correct. I balanced the props. FC is also in correct position , accelerometer calibrated.
PLZ HELP..